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mirror of git://projects.qi-hardware.com/ben-wpan.git synced 2024-11-22 07:04:03 +02:00

More detailed examination of the input circuit problem.

- cntr/README, ecn/INDEX, ecn/ecn0006.txt: moved discussion of the input
  circuit from README to ECN0006
- cntr/cntr.sch: changed pointer from README to ECN0006
- ecn/ecn0006.txt: added more measurements, explanations, and an analysis
  of the situation
This commit is contained in:
Werner Almesberger 2010-11-05 14:45:12 -03:00
parent a8d74345b0
commit 6d4ea61ae1
4 changed files with 136 additions and 30 deletions

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@ -69,34 +69,7 @@ cntr -r; sleep 1 && dfu-util -d 0x20b7:0xcb72 -D cntr.bin
Known issues (version 2 hardware)
---------------------------------
- the input circuit only works up to about 1 MHz. The problem is that
we discharge too slowly though the base of Q1, which in turn keeps
the transistor turned on too long.
An alternative design that sets R2 to zero, adds a 47 Ohm termination
resistor in parallel to VR4, and places a 1 kOhm resistor between
VR4 and Q1 works up to about 2 MHz, but accepts a lot of HF noise
and is very sensitive to the signal amplitude.
Some test results with a ~1.8 m RG-174 cable, square wave bursts
with a 50% duty cycle and ~ 5 ns raise/fall time:
Design Frequency Source amplitude Input amplitude
(nominal) (nominal) (measured)
------------ ---------- ---------------- ---------------
Original 1 MHz 700 mV ~700 mV
Alternative 2 MHz 1.6 V ~800 mV
1 MHz 1.5 V ~750 mV
The test consisted of setting the frequency and adjusting the nominal
source voltage in increments of 100 mV for the lowest voltage at
which which ten consecutive bursts of 50000 cycles each were all
received correctly.
The source has an output impedance of 50 Ohm, so voltage at the probe
input (indicated in the table) is roughly half the nominal source
voltage in the alternative design.
- the input circuit does not perform well. See ECN0006 for details.
- the MMCX connector is hard to solder because of its large thermal
capacitance and surface
- the lateral pads of the MMCX connector could be wider

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@ -1,4 +1,4 @@
EESchema Schematic File Version 2 date Thu Nov 4 21:28:19 2010
EESchema Schematic File Version 2 date Fri Nov 5 14:44:54 2010
LIBS:power
LIBS:device
LIBS:conn
@ -19,7 +19,7 @@ Comment3 ""
Comment4 ""
$EndDescr
Text Notes 8250 1000 0 100 ~ 20
Input circuit has known bugs.\nSee README for details.
Input circuit has known bugs.\nSee ECN0006 for details.
NoConn ~ 8400 3800
NoConn ~ 8400 2900
Wire Wire Line

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@ -5,3 +5,4 @@ Number Status Description
0003 Edit Replace balun and filter with integrated balun
0004 Edit Take into account layout considerations for RF
0005 Edit Correct atusd clock voltage divider
0006 Edit CNTR version 2 input circuit

132
ecn/ecn0006.txt Normal file
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@ -0,0 +1,132 @@
CNTR version 2 input circuit
Problem description
-------------------
The input circuit only works up to about 1 or 2 MHz. The problem is that
we discharge too slowly though the base of Q1, which in turn keeps the
transistor turned on too long.
Attempted solutions
-------------------
The following alternative designs have been tried:
- Alternative 1: set R2 to zero, add a 47 Ohm termination resistor in
parallel with VR4, and place a 1 kOhm resistor between VR4 and Q1.
Works up to about 2 MHz, but accepts a lot of HF noise and is very
sensitive to the signal amplitude.
- Alternative 2: increase R2 to 100 Ohm and add a 100 Ohm resistor
between the input (P5) and ground. This works up to 3 MHz, but only
for a very limited amplitude range.
- Alternative 3: set R2 to zero, add a 100 Ohm resistor in parallel
with VR4, and add a 100 Ohm resistor between VR4 and Q1.
Experimental results
--------------------
Lab test were performed on all version 2 variants and also on a version
1 device. The counters were connected with a ~1.95 m RG-174 cable to a
Picotest G5100A function generator. The version 1 counter was also
tested with an unshielded 0.1" ribbon cable of 2.2 m.
The signal consisted of square wave bursts with a 50% duty cycle and
~ 5 ns raise/fall time.
Design Frequency Source amplitude Probe input am- V range
(nominal) (nominal) pli. (measured) acceptable
------------- ---------- ---------------- --------------- ----------
Version 1 3 MHz 2.3 - 5.5 V * 2.35 - 5.65 V Y/Y
(RG-174) 2 MHz 2.1 - 5.5 V * 2.15 - 5.7 V Y/Y
1 MHz 1.8 - 5.5 V * 1.85 - 5.7 V Y/Y
Version 1 3 MHz 1.9 - 5.5 V * 2.2 - 6.5 V + Y/(Y)
(ribbon) 2 MHz 1.9 - 5.5 V * 1.9 - 6 V + Y/(Y)
1 MHz 1.8 - 5.5 V * 1.9 - 5.7 V + Y/(Y)
Version 2 3 MHz 0.8 - 1.2 V 0.8 - 1.0 V Y/N
2 MHz 0.8 - 1.6 V 0.8 - 1.0 V Y/N
1 MHz 0.8 - 5.1 V 0.8 - 2.8 V Y/Y
Version 2, 3 MHz 1.7 - 2.8 V 0.85 - 1.4 V N/N
alternative 1 2 MHz 1.6 - 3.5 V 0.80 - 1.75 V Y/Y
1 MHz 1.5 - 7.2 V 0.75 - 3.6 V Y/Y
Version 2, 3 MHz 1.2 - 2.0 V 0.77 - 1.1 V Y/N
alternative 2 2 MHz 1.2 - 2.6 V 0.80 - 1.4 V Y/N
1 MHz 1.1 - 7.3 V 0.75 - 3.9 V Y/Y
Version 2, 3 MHz 1.1 - 1.7 V 0.74 - 1.0 V Y/N
alternative 3 2 MHz 1.1 - 2.4 V 0.74 - 1.3 V Y/N
1 MHz 1.1 - 7.3 V 0.74 - 3.8 V Y/Y
* = range limited by maximum input voltage
+ = considerable overshoot, reaching about 6.7 V
The following drawing illustrates the setup:
Source ----- 50 R ----- Probe -----[1.8 m]----- Cntr
^ (internal) ^
| |
Source, nominal Probe input, measured
In each test the frequency was set and then the nominal source voltage
was adjusted in increments of 100 mV to find the range at which ten
consecutive bursts of 50000 cycles each were all received correctly.
The source has an output impedance of 50 Ohm, so voltage at the probe
input (indicated in the table) is roughly half the nominal source
voltage in the first alternative design, which has a fixed impedance.
With version 1, which has a high-impedance input, source and probe
voltage are roughly the same.
The amplitude range of version 2 was considered acceptable if the
minimum source amplitude was less than 1.65 V and the maximum probe
input amplitude was greater than 1.65 V.
Version 1 amplitudes were considered acceptable if the minimum source
amplitude was less than or equal to 2.5 V and the maximum source
amplitude was at least 5.0 V. The ribbon had a better amplitude range
than the coax cable but produced about 20% overshoot. (Only about
10-15% can be considered safe at TTL levels.)
Analysis
--------
None of the attempts at rearranging the resistors produced a
significantly better input circuit. Perhaps a reduction of the
capacitance of VR4 or could have helped, but this was not tried.
I "clean" solution would require a fast comparator. This would also
allow the implementation of a settable threshold voltage, e.g, for
compatibility with 1.8 V logic.
The version 1 board performs extremely well at 3.3 V and 5 V logic
levels, particularly when using a coax cable. For shorter distances,
also a ribbon cable should be adequate.
Conclusion
----------
Revert the input circuit to version 1, with the following changes:
- change R2 from useless 100 kOhm to 1 kOhm or less. Consider
adding a second switchable resistor that can be put in parallel.
- use the same TVS VR4 as for VR1 through VR3, to reduce the BOM
count
- use a 0.1" connector with three contacts instead of two, so that
the signal is in the middle. This will prevent accidental shorts
and it makes it easy to build an adapter to an MMCX jack.