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fc54b9bf15
(stable-branch of Openmoko) git-svn-id: svn://svn.openwrt.org/openwrt/trunk@13613 3c298f89-4303-0410-b956-a3cf2f4a3e73
85 lines
2.7 KiB
Diff
85 lines
2.7 KiB
Diff
From 64ec7be81097f2c02ecffadbb2eef22ccf4c7e7b Mon Sep 17 00:00:00 2001
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From: Mike Westerhof <mwester@dls.net>
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Date: Wed, 16 Apr 2008 20:51:17 +0100
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Subject: [PATCH] gta01-fix-jbt-platform-missing-members.patch
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Created an attachment (id=594) / BZ#79
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Add missing platform_data that caused the GTA01 to crash on suspend/resume
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The interface to the jbt6k74 driver changed slightly; this patch adds the
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missing platform_data for the GTA01. This prevents a crash while suspending.
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This patch also makes some minor changes to cleanup and clarify some debug
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messages.
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Signed-off-by: Mike Westerhof <mwester@dls.net>
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---
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arch/arm/mach-s3c2410/mach-gta01.c | 21 ++++++++++++++++-----
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1 files changed, 16 insertions(+), 5 deletions(-)
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diff --git a/arch/arm/mach-s3c2410/mach-gta01.c b/arch/arm/mach-s3c2410/mach-gta01.c
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index ff08449..a77ed3d 100644
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--- a/arch/arm/mach-s3c2410/mach-gta01.c
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+++ b/arch/arm/mach-s3c2410/mach-gta01.c
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@@ -73,6 +73,7 @@
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#include <asm/plat-s3c24xx/pm.h>
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#include <asm/plat-s3c24xx/udc.h>
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#include <asm/plat-s3c24xx/neo1973.h>
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+#include <linux/jbt6k74.h>
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static struct map_desc gta01_iodesc[] __initdata = {
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{
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@@ -389,7 +390,7 @@ static void gta01_mmc_set_power(unsigned char power_mode, unsigned short vdd)
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int bit;
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int mv = 1700; /* 1.7V for MMC_VDD_165_195 */
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- printk(KERN_DEBUG "mmc_set_power(power_mode=%u, vdd=%u\n",
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+ printk(KERN_DEBUG "mmc_set_power(power_mode=%u, vdd=%u)\n",
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power_mode, vdd);
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switch (system_rev) {
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@@ -499,10 +500,20 @@ static struct s3c2410_ts_mach_info gta01_ts_cfg = {
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/* SPI */
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+void gta01_jbt6k74_reset(int devidx, int level)
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+{
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+ /* empty place holder; gta01 does not yet use this */
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+ printk(KERN_DEBUG "gta01_jbt6k74_reset\n");
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+}
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+
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+const struct jbt6k74_platform_data gta01_jbt6k74_pdata = {
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+ .reset = gta01_jbt6k74_reset,
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+};
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+
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static struct spi_board_info gta01_spi_board_info[] = {
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{
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.modalias = "jbt6k74",
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- /* platform_data */
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+ .platform_data = >a01_jbt6k74_pdata,
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/* controller_data */
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/* irq */
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.max_speed_hz = 10 * 1000 * 1000,
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@@ -641,7 +652,7 @@ static void __init gta01_map_io(void)
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static irqreturn_t gta01_modem_irq(int irq, void *param)
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{
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- printk(KERN_DEBUG "modem wakeup interrupt\n");
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+ printk(KERN_DEBUG "GSM wakeup interrupt (IRQ %d)\n", irq);
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return IRQ_HANDLED;
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}
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@@ -709,9 +720,9 @@ static void __init gta01_machine_init(void)
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set_irq_type(GTA01_IRQ_MODEM, IRQT_RISING);
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rc = request_irq(GTA01_IRQ_MODEM, gta01_modem_irq, IRQF_DISABLED,
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"modem", NULL);
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- if (!rc)
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- printk(KERN_ERR "GTA01: can't request GSM modem wakeup IRQ\n");
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enable_irq_wake(GTA01_IRQ_MODEM);
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+ printk(KERN_DEBUG "Enabled GSM wakeup IRQ %d (rc=%d)\n",
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+ GTA01_IRQ_MODEM, rc);
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}
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MACHINE_START(NEO1973_GTA01, "GTA01")
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--
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1.5.6.5
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