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labsw/LOG: updated with latest results
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labsw/LOG
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labsw/LOG
@ -104,7 +104,7 @@ Milled face plate #0:
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- correct banana jack hole diameter
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Milled face plate #1:
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- changes made
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- changes made:
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- increased engraving depth to 0.5 mm
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- increased banana jack hole diameter to 8.0 mm
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- defects found:
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@ -114,10 +114,46 @@ Milled face plate #1:
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- noticed that the button holes are milled last, after cutting the
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board outline. This explains the poor accuracy.
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--- Mon 2011-09-05 ------------------------------------------------------------
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Milled face plate #2:
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- changes made:
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- board is unclad FR4
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- added a bit more adhesive tape
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- increased banana jack hole diameter from 8.0 mm to 8.1 mm, to
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accommodate also jacks that are at the upper end of the tolerance
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range
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- corrected order of tool paths issues by cameo
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- measurements:
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- board: 104.1-104.2 mm x 35.1 mm (nom. 104.0 mm x 35.0 mm)
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- button hole: 12.5-12.6 mm x 11.3-11.4 mm (nom. 12.6 x 11.3 mm)
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- defects found:
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- tight horizontal fit in the case
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- LED holder have considerable play and retainer rings are loose to
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the point of being useless
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- adhesive tape now sticks almost too well :-) (it was hard to pry
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the board loose after milling)
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Milled face plate #3:
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- changes made:
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- reduced board width from 104.0 mm to 103.6 mm
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- reduced LED hole from 6.9 mm to 6.2 mm
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- problems encountered:
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- raw board wasn't quite large enough for the entire face plate, but
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it seems I missed it by only < 0.1 mm.
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- depth was too shallow, at the cost of the logo
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- measurements:
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- board: 103.8 mm x 35.1 mm (nom. 103.6 mm x 35.0 mm)
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- defects found:
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- LED holder works better but is still a bit wobbly
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- (EE issue) there's a bit of current from 5 V through the opt-coupler
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LEDs to the pull-ups. Work-around: add 10 kOhm in parallel to each
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LED.
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---------------------
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(next run)
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- changes made
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(next PCB run)
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- changes made:
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- made 5V relay traces go clearly for the centers of the respective pins
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- changed DIP hole size from 0.5 mm to 0.8 mm, hole-to-copper ratio from
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2.5 to 2
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@ -131,3 +167,8 @@ Pending:
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- add orientation markings on copper layer for MCU and DIP sockets
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- verify 2512 footprint of 1 W resistors
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- add ground zones
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- solve opto LED current. Three approaches:
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1) add 10 k in parallel to LED (tested workaround)
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2) disable internal pull-ups and add external pull-ups to IN_*
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and to buttons
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3) drive opto LEDs from 3.3 V instead of 5 V
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